| cylinder 2 had 180 psi dry...dang...and I used two different gauge tops. I'm not sure if I mentioned it, but cylinder six still has a drop in rpm during the power balance test, just not as drastic as any of the others. Although the bleeding fuel pressure and misfire support the idea of a leaking o-ring the spark plug is dry and I lubed the crap out of the o-ring, pushed it in by hand and then evenly screwed on the new hex screws. I even went as far as to swap PTUs. I can take a video of the misfire though if anyone would like...
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